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02.04.08
New PATCH release 02.04.08 Changes since 02.04.07: Find correct inflection point
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02.04.07
New PATCH release 02.04.07 Changes since 02.04.06: Bump patch version WPF: Only apply inflection filter if present WPF: Dump information about decisions made PositionScan: Protect against unknown flattop Fix size of distance arrays Remove no longer existing functions Do not abort after interpolating the first opPoint Empty opPoints need to be -1
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02.04.06
New PATCH release 02.04.06 Changes since 02.04.05: Add accidentally stashed change
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02.04.05
New PATCH release 02.04.05 Changes since 02.04.04: Adapt expected distances to values Lower minimum distance for crossing Lower distance check from ramp start to 40ns Try to denoise steepness calculation Cut zero crossings with too low inflections nearby Use named enum for inflection type Extract working point finding into its own class
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02.04.04
New PATCH release 02.04.04 Changes since 02.04.03: Workingpoint: Fix algorithm add double points Workingpoint: Configurable number of 0-crossings WorkignPoint: Steepness should be float
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02.04.03
New PATCH release 02.04.03 Changes since 02.04.02: Use correct raw data window offset Use first region with beam in trigger scan
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02.04.02
New PATCH release 02.04.02 Changes since 02.04.01: Fix wrong comparsion direction in check
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02.04.01
New PATCH release 02.04.01 Changes since 02.04.00: Bump patch version Use non-zero sensitivity for noise calculation PositionScan: use toroid to identify flattop Remove unused TMCB device
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02.04.00
New MINOR release 02.04.00 Changes since 02.03.03: Interface change: Changed SASE properties Add new property for first bunch in SASE Fix "uninitialised variables" compiler warning EOM scan attenuator revert bug on abort Startup automation new FLASH naming added TMCB unreset
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02.03.03
New PATCH release 02.03.03 Changes since 02.03.02: UserStatistics: Log if unexpected beamline
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02.03.02
New PATCH release 02.03.02 Changes since 02.03.01: Initialize TMCB early if used to drive motor Update test files
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02.03.01
New PATCH release 02.03.01 Changes since 02.03.00: build: Install calibration scripts
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02.03.00
New MINOR release 02.03.00 Changes since 02.02.13: op scripts update script updates for the new FW switch to application reset in the new FW Add missing map file for test Fix setup for ADC test ci: Add .jenkinsfile Fix initial values between modules Test: Force backplaneTriggerChannel to be an integer, not a bool Update optical switch test Bump minor version box LLL on FMC25
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02.02.13
New PATCH release 02.02.13 Changes since 02.02.12: prepare for motor at TMCB, select FLTs with beam only for position scan new FMC20, TMCB mapp files, support MD22 at TMCB Force two modules to be always valid
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02.02.12
New PATCH release 02.02.12 Changes since 02.02.11: double to float EOM bias feedback fix, new configs ADCScan: Use correct ADC range (16 bit, not 32) ADCScan: Fix peak selection ADCScan: Use left-most maximum, not right-most ADCScan: Larger range for single-value plots ADCScan: Plot old delay value EOM bias scan, enabled all PLL scans in parallel ADC trigger scan added ADC scan fixes, runs PLLScan: Average over whole ADC range Fix missing include and string copy in log Fix log timestamps Fix hierarchy of PLL control registers Re-add ADC scan device Fix typos ADCScan: Wait after board reset after scan setup ADCScan: Readback check for all ADCs compact samples array to special length added logging function with timestamp added compacted arrival time arrays, minor fixes Test data: Add missing ADC device test: Update config for tests doocs parameters setup script
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02.02.11
New PATCH release 02.02.11 Changes since 02.02.10: Add ADCDelayScan and PLLBaseScan Status: Periodically write sampleFreq and preSamples added DUD and ALL UserStatistics: Clear the per-sase arrival time test: Add missing calibration table for calibration test consistency group fix in calib applier, add BCM latency feedback strenghtening, calibration no change on empty FLT Remove motor device module
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02.02.10
New PATCH release 02.02.10 Changes since 02.02.09: Test: Add AutomatioModule smoke test switch to toroid constant threshold toroid array processing change Automation: Add module CalibrationApplierTest: Use ConnectingDeviceModule persistance workaround CalibrationApplier: Add basic test Toroid: Data is in 4.5MHz pattern, not dense feedback toroid to reprocessed data momtor feedback reset limit feedback alarms CalibrationApplier: Fix reset of calibration table Fix various clang-tidy warnings StatusCollector: PositionScan status changed calibration scripts added unmodified averaging to quality, stronger position scan cuts
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02.02.09
New PATCH release 02.02.09 Changes since 02.02.08: uint size fix
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02.02.08
New PATCH release 02.02.08 Changes since 02.02.07: encoder settle time and offset realignment encoder modes and position hold, motor movememnt loop simplified, LLL invalid bit setting StatusCollector: Fix connection for feedback and motor Re-enable test for status module added position scan previsous position, less vervosity to log, fix cut in position scan analysis calib file lines +1
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02.02.07
New PATCH release 02.02.07 Changes since 02.02.06: Bump patch version encoder drift protection